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LG&E - Controls Upgrade

PCI Skanska generated a tight and inclusive bid specification, developed replacement strategies, participated in vendor evaluations and developed scope of work documentation. LG&E and PCI Skanska encouraged early involvement of plant maintenance, production and leadership in the control vendor selection.

The scope of work included Boiler and Turbine Control, Burner Management System, Scrubber, Data Acquisition, Ash Handling, Coal Handling and miscellaneous Balance of Plant systems.

Over 17,000 I/O points were engineered, installed and controlled. The project was managed in phases with completion of first phase in the fall of 2007, and the balance of the project completed by fall of 2009.

Results

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